Well I procrastinated for about 3 weeks working out the potential leak details and hardware requirements in my head and occasionally buying only what was absolutely necessary at the local hardware store determined to use as much items I could use from my garden parts bin as possible. So yesterday afternoon got board and decided to finally glue the PVC parts together and assemble my DIY 1 gallon canister filter. After assembly I was of course once again motivated and decided to test it out without media since this was just an integrity test. I knew I had given enough thought to creating makeshift water tight fittings that the canister was either going to work without leaks or fail under pressure. After filling the canister with water and attaching the lid I plugged it in and it immediately started working. All I had to do to remove the small amount of air inside was crack one side on the lid cam and the air hissed out. It has now been running for 12 hours continuously with no leaks even though there is negative pressure due the pumps high700 GPH rate of flow water is actually being sucked out of the tank, confirmed by the suction jolt and hicky you receive when you block the intake side with your palm. I pressure tested the canister by blocking the intake and although the canister sides did slightly move inward it never collapsed or leaked. I also did a positive pressure test by blocking the out flow port and the sides moved slightly outward this time but again never leaked or failed. This was extreme testing and would never happen in actual use , however because the pump is so strong there is more negative pressure then I would like on the canister so I will be adding an internal restrictor on the pump itself to better balance out the intake and out flow pressure. The restrictor may be as simple as a plug at the impeller port with a hole drilled to the correct metering size that will control pressure on the pump housing rather then on the canister housing, hoses, or fittings. The best was would be with a voltage regulator that would slow the pump down but that’s outside my DIY budget so far $39.
Below as you can see items pointed out in red not covered in previous post . All fittings that pass through the canister to the outside must be a type of bulkhead compression fitting, The PVC piping using standard ½ inch threaded male female fitting with sandwiched garden hose washers on both sides to create bulkhead pressure fittings. Also the electrical cord passing though a male & female end plug fittings filled with silicone, otherwise known in Naval Engineering as a stuffing tube which allows wires to pass through ships compartments without water being able to get though regardless of pressure because the elongated tube with its small opening at each end large enough only to allow wiring to pass through is filled with sealant and there is not enough square inches to apply pressure and force water past the seal. The sealant you see on the end of the outside fitting and wire was just residue that I will remove now that its cured dry. You will also notice inside the lid a simple PVC T-fitting used as the incoming water diffuser. Also you’ll notice the PVC O-ring hose couplers that couple, uncouple, and seal without effort, instead of regular garden hose fittings which take way too much effort to remove and tighten without leaks.
In this next photo below you will notice my custom “lid to pump push on coupler” . This was the most difficult problem to overcome because all canister filters must find a way to simultaneously close the sealed lid and connect to the sealed pump, all in one action. I had to find just the right size hose and push on fitting that allows me to just line up and push the lid down penetrating the pump hose with the male self sealing shank fitting without disturbing media.
In this next photo below you will see I use PVC 90 degree elbow fittings to create the tank bend and also attached some basic PVC ½ inch pipe extension which still awaits fitting with strainers and extensions, but the basics are done and my DIY canister is working much better then expected in spite be told it would not work.
In this last photo below you will see why floor canisters that depend on siphoned water have limitations. Because the pump has greater flow then gravity siphoning can provide at 14 PSI, negative pressure created inside the canister causes air to un-dissolve out of solution, noted by the unusual bubbles in the photo with tiny bubbles inside them. This is why the Fuval FX-5 has to shut down every 24 hours to purge air, not because its has an air leak but because the powerful GPH causing negative atmospheric pressure inside the canister is pulling out right out of the water itself. This same phenomena is happening with my DIY canister at a rate of 1/10 the canister filling with air every 24 hours. Also of concern is that negative pressure canisters that pull air out of solution means lower oxygenated water being progressively being pumped out of the tank water over time if not compensated with very good aeration. Another reason why I will be installing a restrictor to equalize the pressure and alleviate this problem.
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